The ending photo in the Master Cylinder Repair blog kinda hinted that diving into brake wheel cylinder repair was a chore that needed to jump to the top of the Dodge's to-do list. Here's the photo again:
Today I pulled the offending left rear wheel off and psyched myself up for the chore of getting the brake drum off. They're never easy, but I guess I should Never Say Never. Who would have guessed it would be relatively easy? So the three large countersunk screws seen in the photo below fasten the drum to the hub. I unscrewed the three screws (they weren't super tight) and noticed there are three corresponding threaded holes in the drum to screw the three screws into so the drum can easily be pressed off the wheel studs by tightening the screws. I loosened the brake shoes using the adjustments on the backing plate and the drum slid off with little drama.
I used this big-head stubby Craftsman screwdriver (below) to deal with the three screws. It's from my dad. It's probably from the late '60. The only time I ever saw him use it (and what I used it for when I was old enough) was to open the old style 1-quart oil cans (that you only see in an antique store and my basement anymore). The containers were a thick cardboard middle section with a tin bottom and top. This screwdriver was the right size to poke holes in the lid to pour out the oil into a car engine. Now that I have the screwdriver, it gets used quite often in other ways, and it was the perfect size for those large brake drum screws.
This next photo shows the brake shoe top and bottom adjusters. The top snail-shaped adjusters can only move the "toe" (top) of the shoes out toward the drum or in away from the drum. The bottom adjusters look round but are essentially an eccentric cam and can move the "heel" (bottom) of the shoes in/out and up/down to a small degree. It's really a lot simpler to see them in action that try to describe how they work.
I put the wheel cylinder back together, put the shoes back in place with the spring, and slipped the drum on most of the way, to hold the shoes from spreading apart. I then bled the line and brake fluid gushed out again. Back apart came the wheel cylinder and more honing. Back together, but this time I just put a ratchet strap around the shoes to hold them in place, so I could see where the leak was, if any. Yep, another gusher. Something was definitely not right but I didn't know what, so I called it a day again.
At that point I decided I'd just buy new wheel cylinders, as I figured they'd be maybe $30 at the most. Nope. The cheapest was $44 apiece plus shipping/tax, so that would be over $200 for four cylinders. I then got onto a Facebook Military Vehicle forum I'm subscribed to and searched for anything that might help.
Well, come to find out, because the wheel cylinders are stepped inside (1-1/4" bore on the front side and 1-3/8" bore on the back side), there's a step inside the cylinder (you can see it in the above photo) and with the top shoe adjusters all the way in, the front brake shoe pushes the 1-1/4" rubber cup far enough back in the bore that the rubber cup drops out of the small bore and the seal is lost, so brake fluid can just run out the front of the wheel cylinder. You'd think Chrysler wouldn't have made it so the adjusters could allow the shoes to push the piston/cup in so far.
The solution to this issue, per the FB forum guys, is to crank out the top shoe adjusters maybe halfway so the shoes can't push the 1-1/4" cup into the 1-3/8" bore. I did that the next morning and everything worked great.
On to the left front brake. Cobwebs adorned this brake drum like the previous two. By the way, that is a Superwinch locking hub, probably from the 1980s.
Both pistons were seized tight in the wheel cylinder so I decided to pull the cylinder and work on it on the bench. I had to grind a cheap 1/2" box wrench down so I could loosen the two wheel cylinder bolts, as the steering gear was in the way to fit a full width wrench in (and an open end wrench was goobering up the bolt's hex head). Here's a photo showing the lack of room.
The photo below is me applying heat to the wheel cylinder, to hopefully break things loose.
This next photo is the right front wheel cylinder all done after getting new stones for the hone - again.
The truck is now back together and I took it for a test drive. The brakes worked like a charm. To summarize, out of eight brake shoes on the truck (two for each wheel), one or possibly two shoes were somewhat operational before I rebuilt the wheel cylinders. No wonder the truck barely slowed down when I drove it to and from the tractor show last month. I did plan ahead and anticipated every stop and was never in any danger of running into anything (the truck is just so slow), but it is good to have operating brakes now.
I'd like to mention how I adjusted the brake shoes. I didn't use a 0.006" feeler gauge like the shop manual says to use. I just went by feel. First step was to back off all four adjusters. Next I would adjust one top adjuster until the shoe started dragging on the drum, and then back off the adjuster a little bit until the drum spun again. Next I would adjust the lower adjuster until the brake dragged, and back off a little until the drum spun. Repeat for the second shoe.
7/23/2025 update: Ok, so today I was at a fellow tractor club member's garage sale. Guess what they had that I couldn't live without, and just five days after I finished up this wheel cylinder job? Still in its original packaging. And it was a buck. Who knows when I'll ever need it but I'd be nuts to pass it up.
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